View Single Post
  #13  
Old 10-20-2013, 09:56 PM
ngoma ngoma is offline
Supporting Member
 
Join Date: Nov 2009
Posts: 1,358
Default

It really was the flange that was leaking; the o-ring was squished, hardened, and cracked. Replaced it with a nitrile 22mm ID x 3mm thick o-ring. So it wasn't caused by the fitting hitting the firewall during motor/trans mount replacement.

Starting to see a pattern here. Had to replace the tee (drain valve) fitting under the vacuum pump a couple of months ago. It was crumbling to pieces, could have been catastrophic but caught it blocks from home.
__________________
1985 744 gle d24t
1985 745 gle d24t
Reply With Quote