View Single Post
  #7  
Old 01-21-2016, 11:41 PM
Edubcee Edubcee is offline
Junior Member
 
Join Date: Nov 2015
Posts: 8
Default

Hi
After having more of a play she's back on 6 but still jogging about
I did notice the engine mount fuel pump side is dead so I'll be doing that too as is probably not helping
I did check the clear fuel line and no bubbles the new filter has remained full so I was thinking the water trap on the old filter may have been letting air in or a bad mating seal
Power seems good till 4-4.5k now and trails off but no massive smoke or bad noises ( as quiet as a d24t could be)
I was thinking about temporarily turning up the fuel to get the pump running harder to clear the crud out of it
I take it I just remove the tamper seal turn the screw then adjust idle to suit ( any chance it will try to run away if I adjust)
I figured make it smoke a little take it for a blast then turn it back down
Cheers for all the help
Eddie
Reply With Quote